Today's work on the drone consisted of finishing the ESC wiring to the power board and CC3D flight controller. Controller programming was done through LibrePilot. After enabling the motors via remote control, one motor wouldn't start until high PWM and remained stuck in its state regardless of input. To diagnose, I connected the motor to a different ESC and it worked normally, so I figured the ESC was bad and purchased a new one.
FPV components are on the way:
- Eachine TS5828L 40-Ch Transmitter


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